How I repaired the instrument cluster main plug
Posted: Thu Jun 30, 2011 12:40 pm
With the main harnesses for the Monoshock bikes no longer available, we are left with only two options, repair or replace with a good used one. Finding a good used one is probably more hit and miss, since I don’t know of a quick way to test the harness before installation. The wire for the neutral light was broken in the main plug. I initially did this as a temporary repair, but now realize it’s probably more of a permanent fix. I would have taken more photos had I realized this wasn’t a temporary repair.
What I can say is that the plug is of poor design. The female connectors themselves have a collar at the deep end, which is supposed to keeps them in place. Since rubber is flexible, this unfortunately allows the connectors to move slightly while the wire is fixed rubber. With the wire fixed and the connector moving slightly, breaks are bound to occur. I don’t think this would be an issue if BMW had put each connector in a ridged metal frame. Anyway, I would make sure that both male and female connectors have plenty of dielectric grease.
What I did. I cut into the side of the plug and removed, somewhat carefully, a piece of the rubber, so I could glue it back on. Unfortunately, I wasn’t able to save any of the rubber closer to the affected connector. On the plus side, it’s relatively easy to reuse the connector. I re-routed the wire out the back, then spliced into the wire just south of the main plug. The neutral light is now bright and steady.
If I were to do this again, I might be temped to drill a hole on the back side, then push the affected connector out the back, this would damage the rubber portion of the plug less. The only downside to this approach could be drilling through a wire to a different connector. But, there wasn’t a wire directly behind the connector I cut out, so the risk is most likely minimal. The connector was deformed slightly while removing it, so it’s possible that pushing it out the back would cause less deformation, if at all.
Here are some photos of the repair.
What I can say is that the plug is of poor design. The female connectors themselves have a collar at the deep end, which is supposed to keeps them in place. Since rubber is flexible, this unfortunately allows the connectors to move slightly while the wire is fixed rubber. With the wire fixed and the connector moving slightly, breaks are bound to occur. I don’t think this would be an issue if BMW had put each connector in a ridged metal frame. Anyway, I would make sure that both male and female connectors have plenty of dielectric grease.
What I did. I cut into the side of the plug and removed, somewhat carefully, a piece of the rubber, so I could glue it back on. Unfortunately, I wasn’t able to save any of the rubber closer to the affected connector. On the plus side, it’s relatively easy to reuse the connector. I re-routed the wire out the back, then spliced into the wire just south of the main plug. The neutral light is now bright and steady.
If I were to do this again, I might be temped to drill a hole on the back side, then push the affected connector out the back, this would damage the rubber portion of the plug less. The only downside to this approach could be drilling through a wire to a different connector. But, there wasn’t a wire directly behind the connector I cut out, so the risk is most likely minimal. The connector was deformed slightly while removing it, so it’s possible that pushing it out the back would cause less deformation, if at all.
Here are some photos of the repair.